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      08-04-2021, 09:17 AM   #14
MJ6
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Drives: 2018 M4 ZCP 6MT
Join Date: Apr 2018
Location: Virginia

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2018 BMW M4 ZCP  [10.00]
Quote:
Originally Posted by Commanderwiggin View Post
Looks like you need to find that boost leak and pray your rods stay together. 92% gate on E85, you shouldn't even be looking at the dyno. I'd say Jordan did a pretty good job based on the logs given the situation.
I'm dropping my car off today to have the clutch swapped out and to do a boost leak test, so hopefully the leak is found and addressed.

The rods are honestly one thing that still concerns me; at one point we had it up around 655wtq which is where I figured we'd stay for the sake of safety; why I kept seeing an increase in torque after it was mentioned that we needed to keep it below 680 on the stock bottom end is beyond me. If the WGDC was that high, along with a potential boost leak and torque values above what could be considered safe, why wasn't the plug pulled? Again, we didn't have a chance to finalize the tune due to DME communication issues, but I almost feel like it may have been a saving grace at that point.
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2018 F82 ZCP 6MT: FBO, Kratos KRAS55Bi, EU5 Injectors, Dorch HPFP Lift Kit, Stage 3 LPFP, Bend Calibration Zeitronix ECA-2, BM3 Flex-Fuel Tune by ABP

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Last edited by MJ6; 08-04-2021 at 09:25 AM..
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